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Fall 2008 Design Projects


Feedback from the interns in Honduras has shown that settling is occurring in the slopes at Marcala. This is thought to be occurring because the bottom angle is too shallow and because the exit velocity from the slopes is too low. Some literature review showed that to prevent settling and floc break up, the velocity should be around 5 cm/s. The lower angle for future designs was changed from 10 deg to 30-40 deg.
An algorithm was needed to automate the design of the slopes. After several versions, it was decided that exit ports would be needed at the slope exit. A description of this algorithm can be found here.

Quatro Communidades

The quatro Communidades design was smaller than other recent designs completed. Single width sedimentation tanks were used for the design. This plant will be the first to be designed to include the sedimentation tank slopes, and an exit channel. Details of the design can be found below.

Quatro Communidades Design

Gracias

We began the semester trying out new set-ups for the Gracias community which required a flowrate much higher than previous designs. The results can be seen below.
It was ultimately decided that Gracias would have a triple width sed tank. The variable widths of the sed tank will later be automated to account for higher flowrates.

Gracias Experimental Set ups

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