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This experiment explored the impact of influent water saturated with air supersaturated with respect to atmospheric pressure on floc blanket formation and effluent turbidityperformance. This experiment involved collaboration with the Floating Floc Research Team, who supplied the saturated water that served as the influent water to the process.

Introduction
Our team ran an experiment to investigate the affects of saturated air on floc blanket formation. To do this, our team paired with the Floating Floc research team, who supplied water saturated with air to the process. This experiment is meant to model the effects of having a supersaturated system and the affects i.e. the effects that change in pressure in the transmission line to the plant could have on sedimentation performance due to gas escaping from dissolved gas coming out of solution in the influent water as bubbles.

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This supersaturated water was fed to the apparatus as influent water, where it immediately experienced a pressure drop to atmospheric pressure. While a pressure drop should result in the immediate formation of escaping air bubbles in the liquid, these did not form immediately. This is due to the activation energy required for the bubble to form, which is dependent on the surface tension of the bubble. In order to test bubble formation we observed the experiment qualitatively, looking for bubbles throughout the apparatus. We also monitored effluent turbidity, a value parameter that would reflect the effect of the bubbles on tube settler performance.

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The hypothesis that absorbed air would be released in the apparatus was qualitatively observed by bubble formation. The adverse effects of bubble formation on floc blanket formation and effluent turbidity were supported qualitatively by the cloudiness of the liquid exiting the sedimentation tank effluentthrough the tube settler. It is possible that these air bubbles caused some of the flocs to break up. In addition, it is likely that these air bubbles disrupted broke up larger flocs resulting in smaller floc particles than expected. The velocity gradient controls the transport of flocs that enter the tube settler to the effluent for turbidity measurement. Floc roll-up is characterized based on a force balance.  Due to the fact that smaller floc particles are entering the velocity gradient in the tube settler, which is assumed to be a convex velocity gradient whose peak is closest to the tube settler escape. This gradient controls the velocity of the sedement that enters the tube settler, based on a force balancethe foce balance reveals that these particles are more likely to escape into the effluent, increasing effluent turbidity.

Quantitatively, data collected over twenty four hours showed an increase in effluent turbidity when comparing the experiment experimental run with saturated air to the control experiment. (Show the graphs. ) We ran this experiment on both high and low floc blanket levels. In the high floc blanket formation state the floc blanket level is above the plate settlers. In the low floc blanket formation the floc blanket formation level is below the plate settlers. The presence of air bubbles could break up some floc particles and force floc particles up into the clarified effluent. Floc particles attached to air bubbles could potentially travel through the tube settler when they would normally settle out.

Experiment 1 & 2: Low & High Floc Blanket Formations

Conclusion and Future Considerations

It was expected that these bubbles would disturb the release of saturated air as bubbles in the sedementation column would prevent effective floc blanket formation, permitting more floc particles to leave with the sedimentation column effluent. The bubbles were expected to break up larger flocs and, create smaller, lighter flocs that would leave through the plate settler (due to a force balance velocity gradient analysis) and increase overall effluent turbidity. An increase in effluent turbidity and the appearance of bubbles in the apparatus supported this hypothesis in the experiment on low floc blanket formation. However, for the experiment on high floc blanket formation, the data was not consistent with this prediction. If AguaClara is considering to design a plant which would traverse altitude drops and climbsdesigning additional plants undergoing elevation drops, results from this experiment should be considered.

Future experiments relating to saturated water in the plant could include bubble removal before floc blanket formation. However, the true effects of saturated air on the experiment cannot be fully determined until the hydraulic jump produced by the chemical drop waterfall effect is controlled. When chemicals are dropped into the system, such as alum, they create surface bubblescurrent design of AguaClara linear chemical doser system is ameliorated. It is not well understood whether bubbles created from the falling jets are the potential cause of worsened performance in plate settler effluent or if worsened performance is caused more by the presence of supersaturated air in some plants, or if both are causing worsened performance.